ANALISIS PENANGANAN KERUSAKAN WING ANTI ICING PADA PESAWAT B737-500 DI HANGGAR PT MERPATI MAINTENANCE FACILITY DAN PENYEBAB KEGAGALAN MENGGUNAKAN METODE FAULT TREE ANALYSIS

RIZQI ROMADHONI, MOCHAMMAD (2021) ANALISIS PENANGANAN KERUSAKAN WING ANTI ICING PADA PESAWAT B737-500 DI HANGGAR PT MERPATI MAINTENANCE FACILITY DAN PENYEBAB KEGAGALAN MENGGUNAKAN METODE FAULT TREE ANALYSIS. Tugas Akhir thesis, Institut Teknologi Dirgantara Adisutjipto.

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Abstract

Anti-icing system is a system that aims to avoid ice formation when the aircraft is in the air. The formation of ice in the aircraft is very important because an aircraft flight will pass through the atmosphere which at a certain altitude will experience the formation of ice, this needs to be avoided so as not to cause problems in order to achieve comfort in flight. The formation of ice will cause harm to the aircraft along with the times many aircraft now use ice protection system that is anti icing system. Problems on the anti-icing system occurred when the author performed periodic C-check at the Hangar PT Merpati Maintenance Facility (MMF) on aircraft Boeing 737-500 which problem was found that the indicator on the P5 panel when switch ON Wing anti icing, L VALVE OPEN and R VALVE OPEN slow lights dim and only bright. From this problem the author is interested in discussing and identifying the cause of the problem in the anti-ice wing. In this study, direct observation methods were used to observe and analyze the handling maintenance of Boeing 737-500 Sriwijaya Air in addition to this study also used fault tree analysis methods to obtain the cause of failure from the Boeing 737-500 wing anti ice system and TAI shutoff valve. The result of research on the problem of Boeing 737-500 wing anti-ice system problem is a problem with the TAI shutoff valve. The problem is solved by troubleshooting which refers to AMM 30-11-11. For removal and installation of TAI shutoff valve based on AMM 30-11-11 page 403. Using the fault tree analysis method, with wing anti icing system problems obtained basic event, namely: Control Pressure Port Problem, Motor Fault, Spring Broken, Dirty Pin Connector, Loosen Connector, EICAM Module Trouble, No Source Electricity, Negative Electricity Source, Wiring Problem.

Item Type: Thesis (Tugas Akhir)
Subjects: T Technology > T Technology (General)
Divisions: Institut Teknologi Dirgantara Adisujtipto > D3 Aeronaitika
Depositing User: Mr Mochammad rizqi
Date Deposited: 25 Apr 2024 03:52
Last Modified: 25 Apr 2024 03:52
URI: http://eprints.stta.ac.id/id/eprint/1522

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